The whole story about why I over hauled the engine is in the thread. You'll have to read it all.
Oh, I have certainly read it all! The problem is that was weeks ago. As We know This thread keeps getting revived because of all the notifications to people like myself that pop up in our email and then the link takes a straight to the last post and that is on a separate page which is unscrollable to get back to the very beginning and which would be very cumbersome and time consuming so we just start conversing at that point for getting a lot of what has transpired previously.
Sad, and maybe inefficient, but that is how it pans out.
I do remember now without going back and reading everything, the history on this. I was the one that kind of jumped your crap at the very beginning for rebuilding the engine in the first place and saying it was probably unnecessary.
Remember that big air filter discussion I said is the only way these things ever get worn out and dirt going in the intake etc?? Then, you assured me it wasn't head gaskets but rings and talked about how thin they were and how much excessive 3 to 4 times the limit of ring Gap when you took it apart..
I've never seen this and also find it hard to believe, I still think it was due to dirt being ingested past the air filter or bypassing it.
That's irrelevant at this point though.
So as I just told the other poster that since this was a freshly put together engine, if it was tight, then something was either installed incorrectly the first time, the wrong part, or some other way out of spec.
Now combining the information you gave me in a previous post which I believe was earlier today that when you change the connecting rod everything has been fine since, my theory is that connecting rod was the wrong one.
Did you take that same rod out of that same engine from the same position and put it back in to the same position??
If you didn't change any of the parts in the engine from when you took it apart to when you put it back together and you didn't change the positions of them like accidentally flipping something over or putting it in the wrong position, then there's no way a clearance can change.
But as I said earlier, sometimes things that just can't happen do.
I've stated before that I'm not big on people taking these engines apart because it's almost always a waste of time and money because there are cheaper alternatives but along this path of things that aren't supposed to happen that do..
Just in the past 18 months I had one of these same engines that ran fine but had a terrible knocking noise in it.
I became so intrigued as to what it could be that I decided to spend the hour or so to take it apart and look around.
I thought for sure I would find something obvious.
I had to complete block disassembled with the crank out both Pistons rods camshaft and everything.
Everything looked absolutely perfect.
Nothing was loose on disassembly and the rods weren't loose or floppy and had no signs of wear or damage.
Now, I don't claim to be an expert on these because I don't mess with them because I think it's a waste of time but I do have some pictures of a couple of little scratches on the Piston skirts but nothing from all my years of engine building autos and everything else let me to believe there would be a problem. Wrist pin had a little play in it but again nothing that should make a noise like I was hearing which was kind of a mid-range knock definitely not top in but not bottom in big end of rod sound.
So now the kicker.
I put it back together and fire it up and it sounds exactly like it did before.
That's not unexpected because I didn't do anything and didn't change anything and didn't find anything.
So I run it for maybe a minute or two.
Then I started once or twice again over the next two or three days but never run it for over another minute or so.
Then, I started up and drive it about 100 ft to load it on a trailer and it's still making the same sound.
I shut it off to get the trailer ready for about 45 seconds.
I started back up and as I go to load it on the trailer after 12 seconds run time the noise goes away!
I rev It up I'll let down I stop and start it several times. The noise did not come back!
I loaded on the trailer and haven't seen or heard from it since so I don't know what happened but it was so quiet when it left that if you had not known there was a problem you would never suspect anything.
Weird.