Diesel_Dude08
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- Joined
- Jan 22, 2021
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- 2
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- 6
Hello, I have been working on a predator 9500 inverter generator for a family friend. He requested a full service along with a few small repairs. Customer was telling me that generator has been neglected, and oil hadn't been changed in a long time. The customer runs a concession business and likely uses generator all day. Generator had 1,670 hours on it. Customer also stated that the generator has been backfiring on shutdown. He said that it started doing it a couple months ago intermittently and now it backfires every shutdown. Customer also stated that pull cord had been broken by some kids playing with the generator. (not sure of when) I asked the customer how he had been shutting the generator down and he said he had been flipping the switch rather than turning the fuel shut off dial like you are supposed to. ( Manual claims the shutoff switch is for emergency shut off and you should turn the fuel shutoff dial on front of the generator to shut it off instead. I figured this was the issue, since you are shutting an engine down from decent rpms to nothing but my understanding is that the customer has been using the switch the whole time he has owned it and he claims it only started backfiring a few months ago.
I went on with service as usual, oil change, full carb teardown and cleaning, new air filter, spark plug (gapped), and I tore apart the front of the generator to gain access to the crank so I could spin the engine over to TDC for a valve lash adjustment. (Exhaust valve in spec)( Intake was loose) I put everything back together and ran it (I figured it just needed a valve lash adjustment) Only ran it for about 2 minutes, flipped the switch and no backfire.
Tonight, I tested it again after it got hot ( ran for about 5-10 minutes) and I flipped the switch.... it slowed down and just as the engine came to a stop BOOM!! slight flame shot out as well.
I was wondering if anyone can give me suggestions on diagnosing the issue or what might be causing this? Is it possible that the kids that broke the pull cord pulled it while it was running and the engagement of the recoil on the running engine caused a sheared flywheel key? Would a sheared flywheel key cause a backfire after engine has basically came to a stop? What else are possible causes? Bent valve? Engine does have almost 1,700 hours on it. Could it be blow-by that is causing excess air to move past the piston rings and into the exhaust?
Hoping I don't have to dig in too deeply, I probably have almost 5 hours of work into this unit between tearing the front of it apart, sizing out 0-rings and wheel bearings, and replacing everything. I only charged the guy $40 in labor but I don't want to charge him too much more.
If anybody has any ideas or suggestions.. all help is appreciated!
I went on with service as usual, oil change, full carb teardown and cleaning, new air filter, spark plug (gapped), and I tore apart the front of the generator to gain access to the crank so I could spin the engine over to TDC for a valve lash adjustment. (Exhaust valve in spec)( Intake was loose) I put everything back together and ran it (I figured it just needed a valve lash adjustment) Only ran it for about 2 minutes, flipped the switch and no backfire.
Tonight, I tested it again after it got hot ( ran for about 5-10 minutes) and I flipped the switch.... it slowed down and just as the engine came to a stop BOOM!! slight flame shot out as well.
I was wondering if anyone can give me suggestions on diagnosing the issue or what might be causing this? Is it possible that the kids that broke the pull cord pulled it while it was running and the engagement of the recoil on the running engine caused a sheared flywheel key? Would a sheared flywheel key cause a backfire after engine has basically came to a stop? What else are possible causes? Bent valve? Engine does have almost 1,700 hours on it. Could it be blow-by that is causing excess air to move past the piston rings and into the exhaust?
Hoping I don't have to dig in too deeply, I probably have almost 5 hours of work into this unit between tearing the front of it apart, sizing out 0-rings and wheel bearings, and replacing everything. I only charged the guy $40 in labor but I don't want to charge him too much more.
If anybody has any ideas or suggestions.. all help is appreciated!