I would say that the engine valves (exhaust) are very hot that is where the gas explodes, make you a short wire or even string that you can slow it down just enough speed to keep it running but much lower RPM's that it was running, disconnect the power cords, this will get it time to cool down fast, usually 30 seconds to a minute and you won't get the back fire which is spent gas.Hello, I have been working on a predator 9500 inverter generator for a family friend. He requested a full service along with a few small repairs. Customer was telling me that generator has been neglected, and oil hadn't been changed in a long time. The customer runs a concession business and likely uses generator all day. Generator had 1,670 hours on it. Customer also stated that the generator has been backfiring on shutdown. He said that it started doing it a couple months ago intermittently and now it backfires every shutdown. Customer also stated that pull cord had been broken by some kids playing with the generator. (not sure of when) I asked the customer how he had been shutting the generator down and he said he had been flipping the switch rather than turning the fuel shut off dial like you are supposed to. ( Manual claims the shutoff switch is for emergency shut off and you should turn the fuel shutoff dial on front of the generator to shut it off instead. I figured this was the issue, since you are shutting an engine down from decent rpms to nothing but my understanding is that the customer has been using the switch the whole time he has owned it and he claims it only started backfiring a few months ago.
I went on with service as usual, oil change, full carb teardown and cleaning, new air filter, spark plug (gapped), and I tore apart the front of the generator to gain access to the crank so I could spin the engine over to TDC for a valve lash adjustment. (Exhaust valve in spec)( Intake was loose) I put everything back together and ran it (I figured it just needed a valve lash adjustment) Only ran it for about 2 minutes, flipped the switch and no backfire.
Tonight, I tested it again after it got hot ( ran for about 5-10 minutes) and I flipped the switch.... it slowed down and just as the engine came to a stop BOOM!! slight flame shot out as well.
I was wondering if anyone can give me suggestions on diagnosing the issue or what might be causing this? Is it possible that the kids that broke the pull cord pulled it while it was running and the engagement of the recoil on the running engine caused a sheared flywheel key? Would a sheared flywheel key cause a backfire after engine has basically came to a stop? What else are possible causes? Bent valve? Engine does have almost 1,700 hours on it. Could it be blow-by that is causing excess air to move past the piston rings and into the exhaust?
Hoping I don't have to dig in too deeply, I probably have almost 5 hours of work into this unit between tearing the front of it apart, sizing out 0-rings and wheel bearings, and replacing everything. I only charged the guy $40 in labor but I don't want to charge him too much more.
If anybody has any ideas or suggestions.. all help is appreciated!
interesting... I forgot that carburetor had that on it. I know it wasn't seized at least because I remember moving the plunger up and down with my finger when I rebuilt that carburetor. However, is testing it as simple as pulling out from the carb and turning the power switch on/off and see if it moves up and down? What could be wrong with the muffler to cause that backfiring to happen? (the 9500 does not have a spark arrestor) Thank you for the suggestion!I suspect that part of the issue is the afterfire solenoid on the bottom of the carb isn't working correctly. Either a solenoid issue or the control circuit that actuates it isn't working correctly. On generators, the afterfire solenoid is normally open and then is closed by the generator output on shutdown. Could also be something as simple or complicated as a muffler issue.
I would agree with you about the immediate shutdown without backing down the revs to cause the backfiring... However, the customer stated that he had always shut it down that way and it only started backfiring a couple months ago... which suggests there is something else going on. Of course... I have already recommended shutting it down the proper way with the slow fuel shut-of switch/valve/dial on the front of the generator.I would say that the engine valves (exhaust) are very hot that is where the gas explodes, make you a short wire or even string that you can slow it down just enough speed to keep it running but much lower RPM's that it was running, disconnect the power cords, this will get it time to cool down fast, usually 30 seconds to a minute and you won't get the back fire which is spent gas.
The solenoid gets is power to block the carb jet with the exciter voltage when the switch is turned off. There is no power supplied by the battery or the charge system to close the valve. So the engine has to be running for it to work, which can't be done with it removed from the carb. Maybe able to apply voltage to the solenoid to see if it works, but I don't know what the input voltage is. Could be 6 volts and a 12 volt battery could burn out the coil. Also would need to test voltage coming to the power wire.interesting... I forgot that carburetor had that on it. I know it wasn't seized at least because I remember moving the plunger up and down with my finger when I rebuilt that carburetor. However, is testing it as simple as pulling out from the carb and turning the power switch on/off and see if it moves up and down? What could be wrong with the muffler to cause that backfiring to happen? (the 9500 does not have a spark arrestor) Thank you for the suggestion!
Oh I gotcha.. I was thinking it was ran off battery power like a normal system. Unfortunately its a pain to put multimeter leads on it because the connection is sealed all the way up into the front of the generator which is sealed off with glued foam... fun times lol. I will try to peel back that foam and see if i cant test the voltage going to it when I shut it down. Seems like it could be the culprit. Thank you for your help!The solenoid gets is power to block the carb jet with the exciter voltage when the switch is turned off. There is no power supplied by the battery or the charge system to close the valve. So the engine has to be running for it to work, which can't be done with it removed from the carb. Maybe able to apply voltage to the solenoid to see if it works, but I don't know what the input voltage is. Could be 6 volts and a 12 volt battery could burn out the coil. Also would need to test voltage coming to the power wire.
Maybe able to put a meter in series with the power wire for the solenoid and watch the voltage on shutdown.
ok so I traced the wire wrong and the cable going to the solenoid actually goes over by the starter area up against the generator end. I hooked up my power probe even though I didn't know if it was supposed to be a 12v connection or not. and as you can see in the video both of the lower connectors are reading ground with the switch off... that didn't make any sense to me. When i would flip the switch on the generator to the ON position... the left lower cable read ground and the right lower cable didn't read anything. I then applied voltage to the top right cable leading to the solenoid and I didn't hear it click open or closed. Did I test this properly and the solenoid is shot or am I not testing this correctly? I cant really test what voltage is going to the solenoid because of the sealed connectors. Im 16 and still learning electrical... not sure if it was tested properly?The solenoid gets is power to block the carb jet with the exciter voltage when the switch is turned off. There is no power supplied by the battery or the charge system to close the valve. So the engine has to be running for it to work, which can't be done with it removed from the carb. Maybe able to apply voltage to the solenoid to see if it works, but I don't know what the input voltage is. Could be 6 volts and a 12 volt battery could burn out the coil. Also would need to test voltage coming to the power wire.
Maybe able to put a meter in series with the power wire for the solenoid and watch the voltage on shutdown.
I remember being at the Green Industry Equipment Exposition in Louisville, KY about 4 years ago and asking a guy selling pull start generators with no battery about the solenoid on the carburetor. He didn’t have an answer and I didn’t understand it either. Because these solenoids are the complete opposite of normal ones on how they operate, it makes sense. Pintle on solenoid is normally open, and then goes in to shut off fuel to main jet upon shut down. It is often amazing to me how simple some things are once you understand how they work. Clean the solenoid with carburetor cleaner and hit it with air compressor air gun and it should unstick and start working again.It is best to remove the solenoid for testing, this way you see it operate.
As IL these operate right the opposite of the other solenoids. As you shut down the generator it applies 12v which extends the pin. It is unlike a mower engine version which 12V is applied while the engine is running to retract the pin.
As equipment sits used for long periods these pins gets gummed with old fuel deposits and can't move as intended. Many can be cleaned to restore operate via ultrasonics. But those that have rusted due to water in the fuel has to be replaced. They also fail electrically by opening up or shorting.
Now if someone in the past has replaced the solenoid they may have simply installed the wrong version not knowing how these operate.
Initially, going to this trade show was mainly about gathering, listening, and learning as much as I could from other people about mechanical and technical knowledge on small engines and outdoor power equipment in general. What I quickly found out was that most people do not know much more than the basics. This year when I go to the trade show it is mostly about seeing new products, talking with people, asking questions, but not so much emphasis on learning specifics. It has really improved my confidence by realizing just how far I have come in the 7 years I have running a small engine shop.Tiger, That just should how well informed the salespersons are not. It like when you call tech support and they can't the simple should be known things.
I feel like I am dealing with idiots at times when I ask for help of these support personnel. It like the other day when I needed the PTO end size of a new engine's crankshaft, all they keep giving me was the bolt size.
Over time carbon builds up and that is igniting the gas on shut down. Idle it then shut down should eliminate most of the problem.Hello, I have been working on a predator 9500 inverter generator for a family friend. He requested a full service along with a few small repairs. Customer was telling me that generator has been neglected, and oil hadn't been changed in a long time. The customer runs a concession business and likely uses generator all day. Generator had 1,670 hours on it. Customer also stated that the generator has been backfiring on shutdown. He said that it started doing it a couple months ago intermittently and now it backfires every shutdown. Customer also stated that pull cord had been broken by some kids playing with the generator. (not sure of when) I asked the customer how he had been shutting the generator down and he said he had been flipping the switch rather than turning the fuel shut off dial like you are supposed to. ( Manual claims the shutoff switch is for emergency shut off and you should turn the fuel shutoff dial on front of the generator to shut it off instead. I figured this was the issue, since you are shutting an engine down from decent rpms to nothing but my understanding is that the customer has been using the switch the whole time he has owned it and he claims it only started backfiring a few months ago.
I went on with service as usual, oil change, full carb teardown and cleaning, new air filter, spark plug (gapped), and I tore apart the front of the generator to gain access to the crank so I could spin the engine over to TDC for a valve lash adjustment. (Exhaust valve in spec)( Intake was loose) I put everything back together and ran it (I figured it just needed a valve lash adjustment) Only ran it for about 2 minutes, flipped the switch and no backfire.
Tonight, I tested it again after it got hot ( ran for about 5-10 minutes) and I flipped the switch.... it slowed down and just as the engine came to a stop BOOM!! slight flame shot out as well.
I was wondering if anyone can give me suggestions on diagnosing the issue or what might be causing this? Is it possible that the kids that broke the pull cord pulled it while it was running and the engagement of the recoil on the running engine caused a sheared flywheel key? Would a sheared flywheel key cause a backfire after engine has basically came to a stop? What else are possible causes? Bent valve? Engine does have almost 1,700 hours on it. Could it be blow-by that is causing excess air to move past the piston rings and into the exhaust?
Hoping I don't have to dig in too deeply, I probably have almost 5 hours of work into this unit between tearing the front of it apart, sizing out 0-rings and wheel bearings, and replacing everything. I only charged the guy $40 in labor but I don't want to charge him too much more.
If anybody has any ideas or suggestions.. all help is appreciated!
Well said!The afterfire solenoid is used to prevent fuel from entering the muffler on shutdown. The reason it is used is the exact reason you are having. Don't forget as the unit ages deposits can build up in the muffler and as the engine slows is is still pulling fuel thru the engine, without the solenoid functioning properly. As the fuel passes thru the muffler it mixes with oxygen and gets set off by something hot within the muffler --- so BANG ! As you said the operator is supposed to turn the gas off to shut off the generator that way there is no unburned fuel entering the muffler so no bang. Some generators that I have worked with, especially pull start units, have an antifire solenoid that is open except on shut down. It closes until the generator stops then reopens.
The best way to "fix" the problem is for the operator to shut down as recommended, without him doing that you can replace the muffler to possibly eliminate any hot spots inside the muffler -- but it will start banging after a period of time due to buildup within the muffler.
If you put the meter in series, you better be looking for current, not voltage. A parallel connection(solenoid terminal to ground) is needed for voltage if you also expect the solenoid to operate.The solenoid gets is power to block the carb jet with the exciter voltage when the switch is turned off. There is no power supplied by the battery or the charge system to close the valve. So the engine has to be running for it to work, which can't be done with it removed from the carb. Maybe able to apply voltage to the solenoid to see if it works, but I don't know what the input voltage is. Could be 6 volts and a 12 volt battery could burn out the coil. Also would need to test voltage coming to the power wire.
Maybe able to put a meter in series with the power wire for the solenoid and watch the voltage on shutdown.
I want the positive lead connected between the power side output from the generator and the negative lead connected to the other side of that connector going to the solenoid to check voltage supplied from the windings to the solenoid both for checking for output and that the solenoid isn't open which is series not parellel. generator solenoids have 2 wires that connect to the generator wiring and I suspect is powered the entire time the generator is running but is ground side switched at shutdown.If you put the meter in series, you better be looking for current, not voltage. A parallel connection(solenoid terminal to ground) is needed for voltage if you also expect the solenoid to operate.
Doesn't work like that for generator since there is no throttle control and most don't even have idle down setups. So they are fixed speed and shutdown at full throttle.Backfire is usually caused by a rich exhaust mix in a hot exhaust pipe or muffler when fresh air gets sucked in backwards by a decrease in air flow (exhaust) out of the engine. I get a little pop once in a while if I shut down my B&S 22HP with the throttle wide open and don’t cool down a bit after I finish mowing. Normally I drop to idle for a few minutes, then shut it off. All I get then is the “oop, oop, oop” from the compression relief sucking air through the carb. I just like to cool down my air-cooled engines a bit before shutting down. A hard learned lesson from owning an air cooled engine for the better part of 40 years. Cool down at idle solves and prevents a lot of problems.
Can't do that with generator solenoids because they are normally open and are closed on shutdown, whereas rider fuel solenoids are notmally closed and use battery voltage to hold them open while operating.The easiest and quickest test for the solenoid is to simply unplug it with a hot engine running. If the engine stops and pops, you’ve found the problem. If it doesn’t stop you still found the problem. Likely a stuck or fouled needle valve on the solenoid. Thoroughly clean the carb and the needle/seat of the shutoff solenoid and try again. Honestly, a little pop from the muffler really isn’t a big deal as long as there’s no dry combustible material nearby and the spark arrestor is intact. It may well be the engine is running a little richer from reduced compression caused by normal aging and wear. Just learn to expect it if you shut it down at full throttle. Best bet is to drop to idle for 5-10 minutes before shutting down. See how that goes. I suspect the backfiring has been happening since he started shutting it down at full speed. Maybe not as loud at first, but if the muffler baffling is less effective, then it’s going to make more noise
Almost ALL. new gasoline small engine product's carbs have a fuel shutoff solenoid. You should be completely familiar, but if notHello, I have been working on a predator 9500 inverter generator for a family friend. He requested a full service along with a few small repairs. Customer was telling me that generator has been neglected, and oil hadn't been changed in a long time. The customer runs a concession business and likely uses generator all day. Generator had 1,670 hours on it. Customer also stated that the generator has been backfiring on shutdown. He said that it started doing it a couple months ago intermittently and now it backfires every shutdown. Customer also stated that pull cord had been broken by some kids playing with the generator. (not sure of when) I asked the customer how he had been shutting the generator down and he said he had been flipping the switch rather than turning the fuel shut off dial like you are supposed to. ( Manual claims the shutoff switch is for emergency shut off and you should turn the fuel shutoff dial on front of the generator to shut it off instead. I figured this was the issue, since you are shutting an engine down from decent rpms to nothing but my understanding is that the customer has been using the switch the whole time he has owned it and he claims it only started backfiring a few months ago.
I went on with service as usual, oil change, full carb teardown and cleaning, new air filter, spark plug (gapped), and I tore apart the front of the generator to gain access to the crank so I could spin the engine over to TDC for a valve lash adjustment. (Exhaust valve in spec)( Intake was loose) I put everything back together and ran it (I figured it just needed a valve lash adjustment) Only ran it for about 2 minutes, flipped the switch and no backfire.
Tonight, I tested it again after it got hot ( ran for about 5-10 minutes) and I flipped the switch.... it slowed down and just as the engine came to a stop BOOM!! slight flame shot out as well.
I was wondering if anyone can give me suggestions on diagnosing the issue or what might be causing this? Is it possible that the kids that broke the pull cord pulled it while it was running and the engagement of the recoil on the running engine caused a sheared flywheel key? Would a sheared flywheel key cause a backfire after engine has basically came to a stop? What else are possible causes? Bent valve? Engine does have almost 1,700 hours on it. Could it be blow-by that is causing excess air to move past the piston rings and into the exhaust?
Hoping I don't have to dig in too deeply, I probably have almost 5 hours of work into this unit between tearing the front of it apart, sizing out 0-rings and wheel bearings, and replacing everything. I only charged the guy $40 in labor but I don't want to charge him too much more.
If anybody has any ideas or suggestions.. all help is appreciated!