uIPost the model, type and [ISPOILE[/ISPOILER]code?
Check the valve lash and set it at .003-.005 on the intake and .005 on the exhaust. Vlave lash is critical on the OHV Intek single cylinder engines, especially the intake valve lash. If too much it may not crank through on compression. I've even ran them at .002 with good results. Flywheel key partly sheared will cause the spit back. (but not need in going their yet.
When setting the valve lash by the book be sure you are on the compression stroke and then go 1/4 inch ATDC on the piston. You gauge this with the spark plug out and a rod or something in the spark plug hole to get the 1/4 inch past TDC.
It's quite common after installing new cam for the valve lash (especially the intake) to change during break-in sometimes after only 15-20 hours of operation and require a re-adjust.
If it's still spitting back through the carb set the intake at .005
Q
How was the engine acting before you took it apart?
31C7070603B1081205ZE/ also
917.289031.. but it was runnin ok ,it had gotten really loud and I was searching the web for answers or suggestions and an ole boy said that if my flywheel key was bad that it could cause it to run louder than normal..
So I pulled it in the garage to check the key and to adjust the valves.. after that it wouldn’t spin so I tore it down and replaced the cam shaft..
After I put it together it some how started for just a second or two and died., I noticed that my plug wire wasn’t even connected to the plug., plug was fouled so I put in mew plug and it hasn’t fan or even tried to run since..
I think I’ve answered and added the model..
This thing started out it was running poorly and was bogging down while mowing..
I found a gas cap seal had come apart, so I cleaned the whole fuel system including the carburator.. it was really loud after that and still bogged way down under load..
The Governor did appear to be working correctly so I started there and adjusted the gov with no help but I did find a very weak spring on the gov.. I replaced that and performance came back but it is still louder than all get out., I bought a new muffler and that was another fail.. then I talked to that guy and he also convinced me that my head gasket could be why it was so loud, so I found a bad flywheel key and replaced the head gasket and adjusted the valves which I did at tdc and then it wouldn’t turn over completely so I went after the camshaft which was fine but I replaced it anyways.. that’s when I found out about the valve being open a little from the decompression mech.. wss told that was prolly why I couldn’t crank it completely over..
So that’s the basic story not mentioning the oil change the new plug, fuel filter, and air filter..