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Rio not working with new engine

#1

V

volvoram

Hi everyone, just replaced 23 hp briggs on my La140 with a briggs cdi 2500, now when I back up with pto engaged Rio doesn't work and tries to ground eng out, like its not working, so I bypassed button and it still grounds eng out ???Any ideas???


#2

K

Kenbu

I give up. What's Rio…?

1758377006700.jpeg


#3

Scrubcadet10

Scrubcadet10

Reverse In Operation?
I give up. What's Rio…?

View attachment 71925


#4

Scrubcadet10

Scrubcadet10

Did you have to do any modifications to plugs or wiring or was it plug n play?


#5

V

volvoram

I give up. What's Rio…?

View attachment 71925
Reverse implement operation, let's you back up with blades engaged


#6

V

volvoram

Did you have to do any modifications to plugs or wiring or was it plug n play?
Plug and play, new engine harness had a green wire the old one didn't have ,


#7

Scrubcadet10

Scrubcadet10

Alrighty, wiring diagram time.


#8

StarTech

StarTech

Alrighty, wiring diagram time.
Do you mean something like this?
1758419029482.png


#9

Scrubcadet10

Scrubcadet10

Do you mean something like this?
View attachment 71929
Just what I was unable to find. Lol


#10

V

volvoram

Reverse In Operation?
Yes reverse works fine, replaced drive belt when I did engine replacement


#11

V

volvoram

Yes reverse works fine, replaced drive belt when I did engine replacement


#12

StarTech

StarTech

Yes reverse works fine, replaced drive belt when I did engine replacement
Then why you say you have Reverse Inhibit Operation problem as that only affect when have the PTO in engaged and you try to backup without using the bypass switch? This has nothing to do with engine other than killing the ignition in reverse. And relay stay latch up until you are out reverse.


#13

V

volvoram

Then why you say you have Reverse Inhibit Operation problem as that only affect when have the PTO in engaged and you try to backup without using the bypass switch? This has nothing to do with engine other than killing the ignition in reverse. And relay stay latch up until you are out reverse.
That's the problem, cant back up with the pto engaged with Rio button depressed or even when I bypassed the button, kills the engine either way


#14

StarTech

StarTech

Then the RIO relay is not operating. Either the ground or +12 VDC is not there that operate the relay; or the relay itself is bad.

As for where the relay located, it appears to be in the operator control tower [the section with the steering wheel and control switches]. And it going to tight in there.


#15

V

volvoram

Then the RIO relay is not operating. Either the ground or +12 VDC is not there that operate the relay; or the relay itself is bad.

As for where the relay located, it appears to be in the operator control tower [the section with the steering wheel and control switches]. And it going to tight in there.
I ordered a new relay and seat switch,thanks for the help!


#16

StarTech

StarTech

I ordered a new relay and seat switch,thanks for the help!
Well I see you are just throwing at it as the seat switch has nothing to do the reverse inhibit working as intended. It is just that you can't get the relay to operate to bypass the inhibit mode.

You should always test things before ordering parts that is why I posted the electrical schematic for the mower.

I currently working on a golf cart that parts were thrown at it and the one that did it royally screwed things up. Spent 4 hrs Saturday figuring out what he done. Customer is getting billed at $80 per hour for the labor when it started out with a bad ignition switch. If tests were done first it would cost the customer much less than me having to straighten out the resulting mess.


#17

Tiger Small Engine

Tiger Small Engine

Very frustrating going behind a customer that works on equipment and doesn’t fix it. Then you have to figure out what they have done.


#18

StarTech

StarTech

It isn't like I haven't scream as loud as I can at times or gone out and shot my pond water full of 12 ga holes and then called them idiots privately. After 15 yrs I don't get that angry anymore just charge more for straighten out the mess.

I had one customer many years ago to change out the starter, remote solenoid, the stator and voltage regulator, and the keyswitch to only finally brought it in where I it was a simple 50 cent wire terminal problem. $450 down the drain before my bill for an hour of labor and the 50 cents terminal. My was a 1/6 of he wasted trying to fix it himself. What worst he had thrown away all the good parts he replaced.


#19

V

volvoram

Those parts were only about $20


#20

V

volvoram

Those parts were only about $20
I never saw a schematic posted???


#21

StarTech

StarTech

I never saw a schematic posted???
You might ought to stop skimming threads and read the whole thread as it is posted in post #8 back on September 20th. Skimming threads is why so many unnecessary posts are made after thread is solved. Many posters just read the first post in a thread and immediately to posting a reply.


#22

A

Auto Doc's

You might ought to stop skimming threads and read the whole thread as it is posted in post #8 back on September 20th. Skimming threads is why so many unnecessary posts are made after thread is solved. Many posters just read the first post in a thread and immediately to posting a reply.
That takes too much time.... I'm late for something I don't have to do. LOL


#23

H

hlw49

Never ceases to amaze me how people will post a problem and post what they have done and list the parts they threw at the problem. I just sometimes scratch my head and say what did that part have to do with the problem.


#24

StarTech

StarTech

Never ceases to amaze me how people will post a problem and post what they have done and list the parts they threw at the problem. I just sometimes scratch my head and say what did that part have to do with the problem.
That is the professional in you...I see that all the time and shake my head. If they like wasting time and money I'll be glad to take it.


#25

S

slomo

Now I'm all confused.........


#26

StarTech

StarTech

Now I'm all confused.........
Maybe you should have your head examined like I did recently. ;)

The doctors told they didn't find anything and I said I could had told you that without the MRI.:ROFLMAO:

IF there was I would not have let that 2 ft pull bar hit me in the jaw. Next time I think of doing something for extra safety I will.


#27

A

Auto Doc's

Now I'm all confused.........
Hi slomo,

That is why I mention a while back about people mention by username who they are addressing in a reply.

It's Kind of crazy how this site drops replies all over the place in the thread and not just at the end.


#28

D

denk

so is this machine working now or not? :D


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